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تصميم الترتيب الداخلي الافضل للمصنع باستعمال تقنية التخصيص النسبي المحوسب للتسهيلات (CRAFT) : بحث تطبيقي في الشركة العامة لصناعة الزيوت النباتية / مصنع المامون == The Design of Optimal Layout Using Computerized Relative Allocation of Facilities Technique (CRAFT) - Applied Research In Al - M'Ammon Factory / The General Company For Vegetable Oils Industry
Author name:
تبارك محمود شكر الجبوري
Supervisor name:
ايثار عبد الهادي ال فيحان المعموري | احمد زيدان محمد الشمري
General topic:
Administration and Economics
Specific topic:
Industrial Management
Degree:
Master
University:
University of Baghdad - Faculty Of Administration And Economics
Language:
Arabic
University location:
Baghdad
First pages:
07T3509 - p.pdf
Abstract:
ستند هذا البحث, على تصميم وتطبيق برنامج (تقنية) (CRAFT), بغية اعادة تخصيص مراكز عمل مصنع المامون / الشركة العامة لصناعة الزيوت النباتية, لارتفاع كلف المناولة بين مراكز العمل التي تصل الى (63,026) دينار / اليوم, وطول المسافة الخطية المقطوعة بين مراكز العمل | This research based on design and application a program (Technique) (CRAFT), in order to Re - allocation work centers of (Al - M'ammon Factory / The General Company for Vegetable Oils Industry), the high handling costs that reach to (63,026) dinars / day, and length of the distance travelled between work centers which up to (21,778) m / day. The research aims to reach to optimal layout of the factory. In order to reduce the handling costs and reduce the distance travelled between work centers to a minimum, The technique was applied in two stages : - Stage 1 : - Apply (CRAFT) technique according to the initial layout.Stage 2 : - Apply (CRAFT) technique according to the proposed layout reaching to the optimum layout. The results of these layouts has obtained from these two stages, compared with the result evaluation of the initial layout of the factory. As well as, compare the result obtained from the first stage with the result obtained from the second stage, in order to obtain optimum layout of the factory. After procedure these comparisons, optimal layout achieved for the factory from the second stage. Being reduce the costs of material handling rate (22.6%) of the total handling costs for initial layout. As well as reduce (19.2%) of the total distance for initial layout.The research found a set of conclusions. The most important weakness of the efficiency of the initial factory layout, Which turn causes the wasting and losing of a lot of time and effort jacks and persons who transfer materials, and increasing the overall time of production, is produced in the loss of the factory because of high material handling costs between work centers. This research concluded with several recommendations, the most important work on the application of the new layout, which obtained from the application of technique (CRAFT) in the second stage.